Something happened to my `09 225 Pro XS over the weekend that I haven`t seen listed here or on the BBC 3.0 LITER Merc Board. After several starts and stops during our club TX I turned the key and all kinds of weird sounds and really rough idle started coming from under the hood. Lasted about 10 seconds then cleared up like you flipped a switch. Started a few more times and worked just fine. We fished the rest of the day and were going thru a narrow spot in the river above the 411 bridge inVonore at about 4200 rpm due to traffic. I noticed a change in the way the engine was running, surging a couple of hunded RPM up and down , almost like it was running out of gas, or fire. I eased off a little and made itaround the bend and got the ramp in sight although it was still a couple miles away. I set it down off plane and died pretty quickly. Tried tostart it and would start but immediatly die. I probably ran about 2 minutes after it started messing up and was watching my MercMonitor, the RPM dropped to about 3100, the coolant was steady at 120 degrees but the Voltage was running about 12.1-12.3 erractically. I just bought one of those monster group 31 Platinum Diehards a couple months ago and give it about 7-8 hours of 10 amp charge the nite before. I`m sure I had seen 14.1 on the Monitor early that morning....the 12.1 got my attention. Thought maybe a bad coil would suck that much juice up while going bad. </p>
Since it was under warranty I just loaded it up and took it to My Dealer at Bunch Marine in Harriman Monday morning about 10 AM . I forgot that it was the week before MemorialDay weekend. It was apparent when I walked in the Showroom....everybody was hustling around...even TN SNOW!!. Curtis Bunch was giving orders and walking around with a handful of papers,mumbling about being slammed. I usually try to give Mark Bunch a description of my problem so it doesn`t have to gothru 2-3 people but he wasn`t in sight. So the young man behind the counter took my problem and wrote up the work sheet. I said something about hooking up the `puter to get the info from the motor in case we needed to order some parts. He kinda chuckled and said it wont happen today.Looked me in the eye and said they might not be able to get to it this week.I kinda expected that since they were so slammed and thought Oh Well....it happens. Not a big deal.... I saw Mark in the yard on my way to unhook the boat and he asked me what was up.....I told him what it had done...thought might be a coil. Said that was the most common thing with these motors.. So I made the 50 minute trip back home and resigned myself tobeing without the boat for the weekend. Since I was laid off a couple weeks ago I had planned to do serious fishing this next week or two.</p>
As it turned out the stud that is screwed in the block holding idle pulley for the belt was backing out and when the idler finally got out of line enough it threw the belt. It apparently had been doing it for a little while because the belt was really chewed up. The stud has one of those never ever come off aircraft locking nut on top of the pulley, butthe stud was backing out of the block. this engine only has about 25 hour on it.</p>
About 3 oclock I got a call to get come and get my boat out of the way...it was fixed. </p>
</p>
You can`t beat service like thatemoThumbsup emoThumbsup </p>
Since it was under warranty I just loaded it up and took it to My Dealer at Bunch Marine in Harriman Monday morning about 10 AM . I forgot that it was the week before MemorialDay weekend. It was apparent when I walked in the Showroom....everybody was hustling around...even TN SNOW!!. Curtis Bunch was giving orders and walking around with a handful of papers,mumbling about being slammed. I usually try to give Mark Bunch a description of my problem so it doesn`t have to gothru 2-3 people but he wasn`t in sight. So the young man behind the counter took my problem and wrote up the work sheet. I said something about hooking up the `puter to get the info from the motor in case we needed to order some parts. He kinda chuckled and said it wont happen today.Looked me in the eye and said they might not be able to get to it this week.I kinda expected that since they were so slammed and thought Oh Well....it happens. Not a big deal.... I saw Mark in the yard on my way to unhook the boat and he asked me what was up.....I told him what it had done...thought might be a coil. Said that was the most common thing with these motors.. So I made the 50 minute trip back home and resigned myself tobeing without the boat for the weekend. Since I was laid off a couple weeks ago I had planned to do serious fishing this next week or two.</p>
As it turned out the stud that is screwed in the block holding idle pulley for the belt was backing out and when the idler finally got out of line enough it threw the belt. It apparently had been doing it for a little while because the belt was really chewed up. The stud has one of those never ever come off aircraft locking nut on top of the pulley, butthe stud was backing out of the block. this engine only has about 25 hour on it.</p>
About 3 oclock I got a call to get come and get my boat out of the way...it was fixed. </p>
</p>
You can`t beat service like thatemoThumbsup emoThumbsup </p>