Carl had the misfortune to have ran over a Wal-mart bag and burned his engine up. While it destroyed #5 and #6, we went through and did some modifications to it and he want me to share them with you guys. His engine started out as a 96 2.5L 200 EFI. While EFI does make more power, it takes alot of $$$$ to make them run. So for economy we converted it to carburetors and removed the EFI along with the HEAVY 40 amp chargine system.We bored #5 and #6 and honed the others. Installed all new pistos due to these engines are noted to loose locator pins in the pistons if ever overheated. </p>
Here is a list of modifications that has been done to the engine.....</p>
1) Has been portedto 1.575 and 2.150 on the transfes and finger/boosters..</p>
2) The heads have been shaved down from 38CC to 34CC</p>
3) The front 1/2 had been shaved .050 and stuffed with epoxy.</p>
4) The oil gear passage has been filled up with epoxy to make all the cylinders equal</p>
5) The block has been cut to reveal the finger/ booster port passages</p>
6) The rough castings have been removed from the block</p>
7) We have upgraded to fiber reeds to help performance and save the engine in case one breaks.</p>
8) Removed the EFI and installed a set of WH-22's. For you merc guys you know how good these are.</p>
9) Removed the 40 amp system and installed a 9amp system. This is easier on the engine to spin up to around 7k which this engine is capable of doing. </p>
</p>
Here are the pictures. They have explainations of what is being done. I hope you all enjoy this. If you have any questions please feel free to ask!!!!!</p>
Here is a list of modifications that has been done to the engine.....</p>
1) Has been portedto 1.575 and 2.150 on the transfes and finger/boosters..</p>
2) The heads have been shaved down from 38CC to 34CC</p>
3) The front 1/2 had been shaved .050 and stuffed with epoxy.</p>
4) The oil gear passage has been filled up with epoxy to make all the cylinders equal</p>
5) The block has been cut to reveal the finger/ booster port passages</p>
6) The rough castings have been removed from the block</p>
7) We have upgraded to fiber reeds to help performance and save the engine in case one breaks.</p>
8) Removed the EFI and installed a set of WH-22's. For you merc guys you know how good these are.</p>
9) Removed the 40 amp system and installed a 9amp system. This is easier on the engine to spin up to around 7k which this engine is capable of doing. </p>
</p>
Here are the pictures. They have explainations of what is being done. I hope you all enjoy this. If you have any questions please feel free to ask!!!!!</p>
Attachments
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finger before(1).JPG62.1 KB
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finger after.(1).JPG96.8 KB
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another view(1).JPG79.5 KB
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flack(1).JPG75.5 KB
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P1070511(1).JPG79.1 KB
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oil slot block(1).JPG93.7 KB
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oil slot filled(1).JPG78 KB
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heads(1).JPG88.8 KB
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front 12 after(1)(1).JPG82.2 KB
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preped for epoxy(1).JPG76.9 KB
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intake stuffed(1).JPG83.2 KB
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metal reeds(1)(1).JPG90.3 KB
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fiber reeds(1).JPG90.6 KB
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stuffing front 1(1).JPG99.2 KB